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| FM/DM threads Everything about FM/DM in CoD |
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#1
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S!
Crumpp, still some 17 years left of service, going for the full service time Cleared for +12lbs but not for 5min or at any altitude. As that note says 5min is for +9lbs. Out of curiosity how different is the Merlin III used in Spitfire Mk.I being able to use+12lbs for 5min than Merlin XII on Spitfire Mk.II only cleared for take-off up to 1000ft / 3min? Devil is in the details it seems.. |
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#2
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This topic becomes endless. The posters are repeating the same things ad infinitum, name calling etc. No more info can be found here.
The moderatores should lock this topic. All the info is already here. Let the readers decide for themselves. |
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#3
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Quote:
Not much different from late production Merlin III. Note that the Merlin XX, which is also very similar to the XII (except of course supercharger, which is single gear in XII and two gear in XX) was cleared for +12 emergency boost (5 min, not altitude restriction) was cleared in November 1940. |
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#4
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Quote:
Good luck in your service, S!
__________________
Bobika. |
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#5
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Quote:
That the cut-out will provide +12 boost is obvious, it has the same boost control as the Merlin III and it is also proven by the later amendments. The question that remains is when it was authorized. |
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#6
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S!
Will check the link, thanks Banks |
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#7
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Just found another contemporary source.
Flight Magazine - April 1940
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#8
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An interesting clip on building the Merlin:
Wish the original soundtrack had been kept instead of adding the usual muzak |
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#9
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I'd just like to add a little example of how procedures differed during the war when compared to peacetime/modern times.
Spitfires suffered from a couple of problems that would today result in the grounding of the fleet. Namely the "Skew Gear problem" in Merlins where the skew gear would fail randomly and catastrophically, (this happened to Alex Henshaw a number of times) and the Piston seizures on Packard Merlins - caused by the fact that the piston heads were not machined, to save time, and were left to wear to shape, or in some cases seize as the push rods got bent. Neither of these problems would be acceptable today. They simply could not afford to halt production to find the source of the skew gear problem, so they continued making the engines as was, up until the point that they fixed it. This almost certainly cost lives and certainly cost aircraft. Last edited by winny; 04-26-2012 at 01:12 PM. |
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