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#161
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#162
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Indeed. Positive G maneuver? No way ...
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#163
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That's what I thought. And it had power applied too otherwise there's no way it could retain height.
All I would like to know is if this was an injected engine or Ms Schillings Orifice |
#164
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Looking at the video again the engine was not supplying power when inverted, it was windmilling with the occasional detonation. When he was inverted he was almost certainly bleeding airspeed as he went until he rolled right way up and the engine picked up - quite quickly too. Pretty sure its a carburettor not an injector.
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#165
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The Mk.Va came with a float type carburettor. The Tilly orifice would only have an effect when flying at 12lb boost and 3000 rpm, if you did not do that, it was pretty much meaningless. If you did, however, the engine would continue to work under negative g just fine.
To me it sounds as if combustions stops during the inverted flight and the engine spools back up thereafter, which indicates the behaviour to be typical for a Merlin with a standard float type carburettor. On the other hand the engine spools up quite nicely (though on a very rich mixture) immediately after returning to positive g's, so maybe a fuel flow restrictor (i.e. Tilly orifice) was in place. The Merlin handbook states up to 10 seconds of recovery after a neg g situation, which clearly isn't there. |
#166
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In the isentropic case, (T2/T1) = (P2/P1)^((gamma-1)/gamma) Isentropic Supercharger work = W*Cp*(T2-T1) Actual Supercharger work = (Isentropic work)/(Isentropic Efficiency) Reducing the temperature upstream of the supercharger therefore reduces the supercharger work at fixed supercharger efficiency, and therefore increases the overall efficiency of the machine. Furthermore, because the supercharger temperature ratio is > 1, it follows that the the temperature reduction in the induction manifold will be correspondingly greater than that due to the evaporation of the fuel alone (though in this case the 25 K figure was measured in the induction manifold, the point is that you wouldn't actually get a 25 K temperature drop from direct fuel injection at TDC). |
#167
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#168
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Not a plane handbook / pilot notes, but a Merlin document, which I can't seem to find at the moment. Sorry.
Good point about closing the throttle, slipped my mind and it would indeed limit the problem, but the fuel pump would still flood the engine to some extend. |
#169
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The throttle also had to be closed when negativ g cut out occured. IIRC Reason is that when the throttle remains opened and the fuel flow is restored the engine might overrev as power is regain so quickly that the CSP can't react quick enough.
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#170
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Running engine at max RPM and open throttle softens the flooding by some extent, but recovering with same settings can indeed result in overrev. It is probably better to cut the throttle just before recovery and not the moment cut out occurs - this seems more optimal. |
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