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FM/DM threads Everything about FM/DM in CoD

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  #21  
Old 04-16-2011, 09:18 AM
IvanK IvanK is offline
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You dont call Minimum RPM a cut out ??? ... how much power and thrust do you think the prop/engine RPM combination is putting out with the RPM full scale anticlockwise ? You went from 3000RPM to something less than perhaps 1000RPM in a heartbeat !

Last edited by IvanK; 04-16-2011 at 09:21 AM.
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  #22  
Old 04-16-2011, 09:25 AM
Targ Targ is offline
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Quote:
Originally Posted by IvanK View Post
You dont call Minimum RPM a cut out ??? ... how much power and thrust do you think the prop/engine RPM combination is putting out with the RPM full scale anticlockwise ? You went from 3000RPM to something less than perhaps 1000RPM !
I also did a full neg G induced red out and noticed zero change in performence other than the RPM and boost gauge dropping.

I also notice that if I pushed the stick full forward and to the right it would cut out fast but a quick pull back than full forward and right again the engine would recover and continue on its merry way doing negative G's.

look at the 1 minute mark, odd to me at least.
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  #23  
Old 04-16-2011, 10:00 AM
doghous3 doghous3 is offline
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Even judging by pilot accounts, they mention mis-fire which I presume is the sputter/cough and black smoke. That doesn't happen (or at least didn't to me whilst I was testing it) however you fly, the engine didn't cough black-smoke once.
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  #24  
Old 04-16-2011, 10:27 AM
IvanK IvanK is offline
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"zero change in performence other than the RPM and boost gauge dropping."

RPM dropping to full minimum and Boost dropping to zero and even less IS an immense loss of performance !
The Engine has gone from producing full Combat Output to next to nothing. Boost and RPM is a measure of engine performance. .... thats a Cut to me.

Here is my attempt negative G throughout until the recovery.


Last edited by IvanK; 04-16-2011 at 10:30 AM.
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  #25  
Old 04-16-2011, 10:38 AM
Wolf_Rider Wolf_Rider is offline
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at what G is this happening at though?
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  #26  
Old 04-16-2011, 10:38 AM
Sauf Sauf is offline
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I havent as yet tried any of the RAF a/c but have been following the arguments, Viper2000 posted this in the other thread, has anyone had a chance to compare in game (25 sec's in)?




Last edited by Sauf; 04-16-2011 at 10:41 AM.
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  #27  
Old 04-16-2011, 11:02 AM
Viper2000 Viper2000 is offline
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Quote:
Originally Posted by Wolf_Rider View Post
erm... where?
Try this from page 10 of the thread, complete with diagram.

The analysis linked to above only talks about mixture strength, and not the effects of that mixture strength on the engine.

During the lean cut, power initially falls away a bit slower than fuel flow because the design point was rich of stoichiometric, and therefore the temperature rise per unit fuel flow goes up. EGT would also initially rise. There might be incipient detonation, followed by misfiring as the mixture becomes too weak to support combustion (cylinder to cylinder variations in temperature and mixture strength mean that this behaviour will not affect all of the cylinders at the same time).

The lean cut will be less severe at lower power output under reduced positive g because fuel flow is less and so the fuel in the small chamber will therefore last longer; indeed at high altitude the engine might just go straight to rich cut. (Under negative g the small chamber empties much faster because fuel flow can escape from the holes in the small chamber which were provided to admit it.)

During the rich cut, power output falls because the Fuel:Air Ratio is approximately 2.4 times design point (which was already somewhat rich of stoichiometric for high power running). This lowers the combustion temperature considerably which kills the engine's BMEP.

However, combustion will continue because there is still oxygen and a source of ignition in the combustion chamber - the chemistry just changes so that it makes CO, H20, sundry cracked petroleum products, and of course some carbon (soot).

Boost shouldn't initially change during the cut unless engine rpm starts to fall, because the ABC doesn't know anything about the cut, and the supercharger pressure ratio is simply a function of its rpm; since it is geared to the engine.

Therefore, the chain of events is
  1. Power reduction
  2. Possible rpm reduction
    • Boost reduction

The rich cut is worse at lower engine power outputs because the fuel flow from the pumps is a fixed function of rpm, whilst the amount of fuel needed by the engine is a function of power.

At 30000' where the engine is only capable of producing about 500 bhp instead of nearly 1300 at its +12 psi FTH, the fuel flow during the cut would be 2.4*(1300/500) ~ 6.24 times that actually required by the engine. This is such a severe over-rich case that nett power output might fall to zero or even go negative (the prop will obviously windmill, so the engine won't stop; as long as it keeps turning the mags will keep going and so there will still be a spark and therefore recovery will follow).

Recovery time to float-controlled operation upon return to positive g would probably be longer at higher altitudes because the recovery depends upon the rate at which the carburettor can dispose of the excess fuel in the float chamber. This depends upon how much fuel can be carried away by the airflow through the venturi (which is mostly a function of ambient conditions & engine rpm; fuel temperature will also have a 2nd order effect).

At or below FTH, with the mixture about 2.4 times as rich as it should be, power will probably fall to about 1/3rd of the expected value, or perhaps a little less. I could do a cycle analysis if there is sufficient interest; the main unknown is the design point Fuel:Air ratio; I can't lay my hands on my copy of The Performance of a Supercharged Aero-Engine by Hooker et al at the moment...

Last edited by Viper2000; 04-16-2011 at 11:04 AM. Reason: formatting
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  #28  
Old 04-16-2011, 11:10 AM
DC338 DC338 is offline
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Feel like your banging your head up against a wall Ivan?

People if you don't think that it is effecting your performance go to wonder woman view roll upside down an keep at -1G and watch what happens to your airspeed.

It could perhaps do with a little bit more of a cough but it is definitely better than before.
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  #29  
Old 04-16-2011, 11:29 AM
Wolf_Rider Wolf_Rider is offline
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Thanks there Viper, but that didn't quite get to the Ivank's pilot's quotes.

I had noticed earlier though in that thread, the references to the "general pilot's notes1943".






remember, this is late 1940 era, not '41/ '42/ or '43
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  #30  
Old 04-16-2011, 01:54 PM
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Moggy Moggy is offline
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Quote:
Originally Posted by Wolf_Rider View Post
Thanks there Viper, but that didn't quite get to the Ivank's pilot's quotes.

I had noticed earlier though in that thread, the references to the "general pilot's notes1943".






remember, this is late 1940 era, not '41/ '42/ or '43
Slow down there Tiger! Although the notes I provided were from 1943 a lot of it (not all) is still applicable to 1940. The reason is simple, the British were still using 1940 aircraft in 1943. Not as frontline aircraft but in O.T.U. schools for training. In the 1943 FAA training film Fleet Fighter, the pilots are trained on Mk.I Hurricanes.
So naturally, a trainee pilot will need notes for aircraft from 1940 through to 1943.
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